Web
Analytics Made Easy - Statcounter
fflyingdog's Content - Page 7 - The Lotus Forums - Official Lotus Community Partner Jump to content


fflyingdog

Basic Account
  • Posts

    962
  • Joined

  • Last visited

  • Days Won

    3

Posts posted by fflyingdog

  1. Picked the car up today and what happened was that the waste gate rod had worn and caused itself to partially sieze under certain conditions hence causing the car to over boost and eventually destroy the turbine(see pic) .So if i had taken notice of when the car started to over boost more than previously and checked the waste gate rod with some thing as technical as a spanner i would have noticed that it wasn't  free and  smooth and not hanging up i would have saved myself a few bob.

     

     

    http://s131.photobucket.com/user/fflyingdog/media/CameraZOOM-20150429120550609.jpg.html?sort=3&o=0

     

    http://s131.photobucket.com/user/fflyingdog/media/IMG_1413.jpg.html?sort=3&o=1

  2. I fitted a genuine Lotus spec cap,as i said it did sort the problem out.I'm sure you can probably get a non genuine part if you have part number ,maybe there is one on your cap?(assuming it has the correct spec part fitted)

     

    Just had a look in parts manual it states part number .   A082K6042F

  3. Yep i think the culprit(s) ,are a chipped engine and a free flowing exhaust and an over speed,but to be fair this one did last 8 years.Currently working on a solution,one being de-chipping,i did notice it was over starting to over boost a fair bit,one of those ,'i must get around to looking at that ' things.My car is like a beautiful woman when she is good she is very very good  and conversely when she s bad she is expensively bad.Suck it up and move on. (i do hope my Mrs doesn't read this) 

     

    Eta .To correct appalling spelling

  4. As per title ,popped my turbo yesterday after a 'spirited' over take ,lots of smoke and a whining sound followed by a sinking heart and a depleting wallet.These cars test the patience of a saint,when they are good they are very very good but when bad....garage is of course trying to determine cause of failure i am errring towards wastegate actuator but will wait for diagnosis.

     

     

    Nick S4s (less) 

     

    ETA. I mean 5th Turbo not 3rd........my mind was obviously trying to be kind to me 

  5. Update,fitted second hand 'new' gauge works a treat,also heli coiled errant engine mounting bolt,what a diffence a tight engine makes! I really should hang my head in shame for not addressing earlier.

    Eta.Spelling and various words missing.

  6. Found it,it is behind the r/h quarter light panel sits almost on the tank,vac pipe was in good condition ,electrical connections and wire really shabby (looks like heat damage),but gauge does flicked when pulling connector off ,so i,m erring towards a bad transducer.may take it off whilst repairing wiring and give it a technical clout ,if i bridge the two connection's will the gauge just go to full deflection does any one know??

  7. My boost gauge has gone all 'floppy' it sets at rest far over to the left of gauge, but when boosting i am only seeing .5 bar (but i know by the feel etc that it is fully boosting so no problem there) anyone have any ideas,maybe the gauge has just died?

     

     

    Hmmm come to think of it when the car over boosts which does happen occasionally the needle flicks like a mad thing.....so i'm thinking busted gauge.

×
×
  • Create New...

Important Information

We use cookies to enhance your browsing experience, serve personalized ads or content, and analyze our traffic. By clicking " I Accept ", you consent to our use of cookies. We have placed cookies on your device to help make this website better. You can adjust your cookie settings, otherwise we'll assume you're okay to continue.