What an evening, small job (maybe the last of the actual strip down?) and it’s bitten me.
Simple job to strip the dash-crash bar of its rolling boot lock mechanism so that I can get the bar itself powder coated and the boot lock rotating bit painted to neaten it / protect it from rust.
Won’t be seen once back in but a bit grubby and keeps my hand in.
WHAT A SWINE!
Various relays etc off no problem, got half a self tapper out then one end of the bar mount.
The other - no way.
Eighth of a turn, backwards and forwards - no joy.
Got heat on him, no joy.
Tried to fill it from the other end with oil - nah.
Eventually conceded defeat and drilled 2X small holes into the bar just above where I hope the thread goes (other side does) and doused internally with oil and left to marinade.
New oil can left by previous house owner - waste of time, put more back on me than in the work space.
Hopefully can tease it out and not shear the bolt, as that turns it into a repair job - but was tempted to force it thus as my new drill can probably allow me extract the stud if I did.
Reckon the captive bolt bit has really expanded in the tube after being left so long.
Plus point is I’ve finally freed up some desk space and inspired by a few of you guys I’m going to try and do a bit as often as possible to start the ball rolling again after the house move.
This will include repairing the binnacle GRP where it got cut for a switch start to be inserted and then preparing the instruments for remounting as a module.
Idea is to get multi block loom in place so I can remove the complete binnacle if needs be when the refit starts a bit more quickly like on an S3.
Also got a monkey bike resto on the go for a similar period of time and I’m going backwards and forwards between the 2 now to keep my spirits up if a job gets too tough….